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Connecting i2c device on voxl2

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  • A Aaky

    @Alex-Kushleyev Thanks for the response and brief description of m0065 outputs. Highly appreciated. So even when we select Channel function as some other actuator like Gripper still Onshot is used over output lines? Was the previous M0065 firmware also oneshot based or this firmware has changes?

    We are providing seperate 5V power supply to servo from BEC. We are changing the servo from analog to digital in order to confirm the behaviour and will get back to you.

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    Aaky
    Regular
    wrote on last edited by Aaky
    #29

    @Alex-Kushleyev One more help is essential,
    For my gripper control from joystick or in mission modes, there is one module in PX4 at this link . Payload deliverer I tested in SITL, where if I allocate joystick buttons to Gripper open and gripper close, and if I allocate Channel 5 (say) to gripper, then the PWM are published over those channel in order to operate any actuators. (Verified this by looking at SERVO_OUTPUT mavlink message in QGC mavlink inspector)

    Whereas I added payload delivere module in voxl-px4 firmware and I got the gripper related parameters also in QGC which ensured module has been loaded successfully and also I verified in the logs, still when I toggle joystick gripper open close it dosent publish PWM on VOXL2_IO channel 5 allocated to gripper, but actuator tab operates well. Any clue what must be missing? I beleive payload_deliverer is not listening to gripper related commands or voxl2_io is not connected to payload deliverer module. Let me know if you have any clues.

    Alex KushleyevA 1 Reply Last reply
    0
    • A Aaky

      @Alex-Kushleyev One more help is essential,
      For my gripper control from joystick or in mission modes, there is one module in PX4 at this link . Payload deliverer I tested in SITL, where if I allocate joystick buttons to Gripper open and gripper close, and if I allocate Channel 5 (say) to gripper, then the PWM are published over those channel in order to operate any actuators. (Verified this by looking at SERVO_OUTPUT mavlink message in QGC mavlink inspector)

      Whereas I added payload delivere module in voxl-px4 firmware and I got the gripper related parameters also in QGC which ensured module has been loaded successfully and also I verified in the logs, still when I toggle joystick gripper open close it dosent publish PWM on VOXL2_IO channel 5 allocated to gripper, but actuator tab operates well. Any clue what must be missing? I beleive payload_deliverer is not listening to gripper related commands or voxl2_io is not connected to payload deliverer module. Let me know if you have any clues.

      Alex KushleyevA Online
      Alex KushleyevA Online
      Alex Kushleyev
      ModalAI Team
      wrote on last edited by
      #30

      @Aaky , yes the latest M0065 firmware is using OneShot style pulses, which is better for all modern ESCs. Please try the digital servo as you are already planning to do.

      I am not familiar with the joystick setup in PX4. As long as the actuator test is working, it means the signal from the mixer is getting to voxl2_io driver and the correct command is sent to M0065 board and executed. It seems your joystick driver may not be sending out the correct command to the mixer.

      Alex KushleyevA 1 Reply Last reply
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      • Alex KushleyevA Alex Kushleyev

        @Aaky , yes the latest M0065 firmware is using OneShot style pulses, which is better for all modern ESCs. Please try the digital servo as you are already planning to do.

        I am not familiar with the joystick setup in PX4. As long as the actuator test is working, it means the signal from the mixer is getting to voxl2_io driver and the correct command is sent to M0065 board and executed. It seems your joystick driver may not be sending out the correct command to the mixer.

        Alex KushleyevA Online
        Alex KushleyevA Online
        Alex Kushleyev
        ModalAI Team
        wrote on last edited by
        #31

        If you really need to try the periodic (standard, not OneShot PWM), i can add an option to use that.

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        • Alex KushleyevA Alex Kushleyev

          If you really need to try the periodic (standard, not OneShot PWM), i can add an option to use that.

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          Aaky
          Regular
          wrote on last edited by Aaky
          #32

          @Alex-Kushleyev Thanks Alex. I will let you know if PWM instead of Oneshot is to be tried out. I am yet to test Digital servo.

          Also regarding joystick setup, it works only after armed in any flight mode. Thanks for your inputs in this.

          Alex KushleyevA 1 Reply Last reply
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          • A Aaky

            @Alex-Kushleyev Thanks Alex. I will let you know if PWM instead of Oneshot is to be tried out. I am yet to test Digital servo.

            Also regarding joystick setup, it works only after armed in any flight mode. Thanks for your inputs in this.

            Alex KushleyevA Online
            Alex KushleyevA Online
            Alex Kushleyev
            ModalAI Team
            wrote on last edited by
            #33

            @Aaky , yes i saw that if not armed, all the actuators are disabled. I think it is a PX4 "feature" and i am not sure if you can bypass it. If you figure out how, please let us know!

            A 1 Reply Last reply
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            • Alex KushleyevA Alex Kushleyev

              @Aaky , yes i saw that if not armed, all the actuators are disabled. I think it is a PX4 "feature" and i am not sure if you can bypass it. If you figure out how, please let us know!

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              Aaky
              Regular
              wrote on last edited by
              #34

              @Alex-Kushleyev Yes I am trying to see before arming how to get gripper control. Also with digital servo M0065 Oneshot works well without any jitter. So thank you once again for that update.

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              • A Aaky

                @Alex-Kushleyev Yes I am trying to see before arming how to get gripper control. Also with digital servo M0065 Oneshot works well without any jitter. So thank you once again for that update.

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                Aaky
                Regular
                wrote on last edited by Aaky
                #35

                @Alex-Kushleyev We came across extremely weird problem and our aircraft crashed on ground from height of 10 meters due to this. All the actuator outputs saturated and started to vary between 0 to 100% throttle. Please have a look at our log file below. We were comfortably flying UAV for ore then 60 mins in multiples flights, but all of sudden while navigating at high speeds in mission mode, our aircraft crashed.
                Note : After this flight now our aircraft isnt able to takeoff at all, motors dosent seem to be providing enough thrust. Somehow we dont know if its ESC's fault or M0065. We are thinking to replace ESC and check again or maybe Capacitor over ESC gone bad.
                Let me know if you have any clue. Please look at the flight towards the very end.
                Log : https://review.px4.io/plot_app?log=9032c82a-421a-4f25-8fe5-30bff45cadf0

                Alex KushleyevA 1 Reply Last reply
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                • A Aaky

                  @Alex-Kushleyev We came across extremely weird problem and our aircraft crashed on ground from height of 10 meters due to this. All the actuator outputs saturated and started to vary between 0 to 100% throttle. Please have a look at our log file below. We were comfortably flying UAV for ore then 60 mins in multiples flights, but all of sudden while navigating at high speeds in mission mode, our aircraft crashed.
                  Note : After this flight now our aircraft isnt able to takeoff at all, motors dosent seem to be providing enough thrust. Somehow we dont know if its ESC's fault or M0065. We are thinking to replace ESC and check again or maybe Capacitor over ESC gone bad.
                  Let me know if you have any clue. Please look at the flight towards the very end.
                  Log : https://review.px4.io/plot_app?log=9032c82a-421a-4f25-8fe5-30bff45cadf0

                  Alex KushleyevA Online
                  Alex KushleyevA Online
                  Alex Kushleyev
                  ModalAI Team
                  wrote on last edited by
                  #36

                  @Aaky , it looks like your motor 4 (black) was operating at maximum output (1.0) for some time (when the battery voltage got lower and lower) and i suspect that it just could not maintain attitude (roll / pitch) control because the motor 4 was saturated and the drone flipped over. If the actuator saturation occurs, the drone cannot maintain stability. I can take a look at the log more carefully later, but that seems like the issue. Did the drone flip over first then fell? The actuator saturation can be caused by imbalance in center of gravity, since other motors are not saturated. but also it looks like at the low battery voltage there is not much extra margin of thrust for sufficient control.

                  e7433a59-6977-413f-8a8c-94790be2dce5-image.png

                  A 1 Reply Last reply
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                  • Alex KushleyevA Alex Kushleyev

                    @Aaky , it looks like your motor 4 (black) was operating at maximum output (1.0) for some time (when the battery voltage got lower and lower) and i suspect that it just could not maintain attitude (roll / pitch) control because the motor 4 was saturated and the drone flipped over. If the actuator saturation occurs, the drone cannot maintain stability. I can take a look at the log more carefully later, but that seems like the issue. Did the drone flip over first then fell? The actuator saturation can be caused by imbalance in center of gravity, since other motors are not saturated. but also it looks like at the low battery voltage there is not much extra margin of thrust for sufficient control.

                    e7433a59-6977-413f-8a8c-94790be2dce5-image.png

                    A Offline
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                    Aaky
                    Regular
                    wrote on last edited by Aaky
                    #37

                    @Alex-Kushleyev thanks for your analysis Alex. Yes drone did flip but it flipped on ground if I remember correctly. Motor 4's saturation might have caused bit of saturation in other motors as well. But very weird problem is now aircraft isn't able to takeoff even at full battery condition. What can be the problem? Is it possible any components involving ESC or ESC itself damaged?

                    Alex KushleyevA 1 Reply Last reply
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                    • A Aaky

                      @Alex-Kushleyev thanks for your analysis Alex. Yes drone did flip but it flipped on ground if I remember correctly. Motor 4's saturation might have caused bit of saturation in other motors as well. But very weird problem is now aircraft isn't able to takeoff even at full battery condition. What can be the problem? Is it possible any components involving ESC or ESC itself damaged?

                      Alex KushleyevA Online
                      Alex KushleyevA Online
                      Alex Kushleyev
                      ModalAI Team
                      wrote on last edited by
                      #38

                      @Aaky , hmm not sure. You should look at the px4 logs of the takeoff attempts after crash and see what the actuator outputs look like. Also try manual mode (thrust, attitude) if you are comfortable flying (instead of position / height control - not sure which one are you testing now)

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                      • Alex KushleyevA Alex Kushleyev

                        @Aaky , hmm not sure. You should look at the px4 logs of the takeoff attempts after crash and see what the actuator outputs look like. Also try manual mode (thrust, attitude) if you are comfortable flying (instead of position / height control - not sure which one are you testing now)

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                        Aaky
                        Regular
                        wrote on last edited by
                        #39

                        @Alex-Kushleyev Here is the log of flight after this crash where aircraft wasn't able to takeoff.
                        We tried in Altitude mode as well as in position mode by increasing throttle upto 80% still aircraft didn't takeoff.
                        Log : https://review.px4.io/plot_app?log=84d281b9-2756-45c3-b064-ea38848f8580

                        This shouldn't be M0065 problem right? Just wanted to eliminate the variables.

                        Alex KushleyevA 1 Reply Last reply
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                        • A Aaky

                          @Alex-Kushleyev Here is the log of flight after this crash where aircraft wasn't able to takeoff.
                          We tried in Altitude mode as well as in position mode by increasing throttle upto 80% still aircraft didn't takeoff.
                          Log : https://review.px4.io/plot_app?log=84d281b9-2756-45c3-b064-ea38848f8580

                          This shouldn't be M0065 problem right? Just wanted to eliminate the variables.

                          Alex KushleyevA Online
                          Alex KushleyevA Online
                          Alex Kushleyev
                          ModalAI Team
                          wrote on last edited by
                          #40

                          @Aaky, in your first flight, your actuator controls (thrust) was above 0.5 when vehicle took off:

                          165b6380-dcfd-41c9-bbf0-fce561cc6c46-image.png

                          But in your last test (you were in altitude control mode), the thrust barely reached 0.3 - that is not enough for vehicle to take off. That is why i was suggesting to test in thrust / angle mode (not altitude hold).

                          c5945927-c01d-4853-9655-88db5fa3b61c-image.png

                          Also, your motor outputs are quite noisy, perhaps the flight board became loose after the crash, not sure.

                          d5e8b416-14cc-4528-9587-17a88dfd2744-image.png

                          A 1 Reply Last reply
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                          • Alex KushleyevA Alex Kushleyev

                            @Aaky, in your first flight, your actuator controls (thrust) was above 0.5 when vehicle took off:

                            165b6380-dcfd-41c9-bbf0-fce561cc6c46-image.png

                            But in your last test (you were in altitude control mode), the thrust barely reached 0.3 - that is not enough for vehicle to take off. That is why i was suggesting to test in thrust / angle mode (not altitude hold).

                            c5945927-c01d-4853-9655-88db5fa3b61c-image.png

                            Also, your motor outputs are quite noisy, perhaps the flight board became loose after the crash, not sure.

                            d5e8b416-14cc-4528-9587-17a88dfd2744-image.png

                            A Offline
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                            Aaky
                            Regular
                            wrote on last edited by Aaky
                            #41

                            @Alex-Kushleyev Thanks Alex. Can you also send me M0065 firmware with normal PWM outputs on 8 channels of actuators? Maybe a switch over existing firmware with capability to switch between Oneshot vs PWM as you told before.
                            I tried flying today but aircraft is having serious vibrations which didn't exist on our previous flights. We have used dampeners still vibration and controls look very rough. I might just try with normal PWM also once.

                            Alex KushleyevA 1 Reply Last reply
                            0
                            • A Aaky

                              @Alex-Kushleyev Thanks Alex. Can you also send me M0065 firmware with normal PWM outputs on 8 channels of actuators? Maybe a switch over existing firmware with capability to switch between Oneshot vs PWM as you told before.
                              I tried flying today but aircraft is having serious vibrations which didn't exist on our previous flights. We have used dampeners still vibration and controls look very rough. I might just try with normal PWM also once.

                              Alex KushleyevA Online
                              Alex KushleyevA Online
                              Alex Kushleyev
                              ModalAI Team
                              wrote on last edited by
                              #42

                              @Aaky , Sure we can try it, but i suspect the PWM output may not be an issue if it did not have the vibration right before the crash.

                              I do not have the firmware with this change ready to go, but it is an easy switch. I need to test it first and i can provide it to you tomorrow.

                              Meanwhile, I suggest to you to do a thorough inspection of the frame. You can also an actuator test (without propellers) to make sure the motor output seems smooth, at least when you are not flying.

                              When I looked at the original log with the crash, it seemed to me that the gyro vibrations were a bit high, resulting in motor outputs to be noisy as well. Perhaps after a crash something changed (became more loose) and the vibration worsened, pushing the performance past the point of stability.

                              Please make sure that any cables that connect to VOXL2 are not tight, which can cause vibration to travel via cables or even pull on the cables if another component is loose on the frame.

                              I am not sure how much PID tuning you have done, but if the D gain on attitude control is set too high with noisy gyro, this will cause the noisy motor commands to be sent to motors.

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                              • Alex KushleyevA Alex Kushleyev

                                @Aaky , Sure we can try it, but i suspect the PWM output may not be an issue if it did not have the vibration right before the crash.

                                I do not have the firmware with this change ready to go, but it is an easy switch. I need to test it first and i can provide it to you tomorrow.

                                Meanwhile, I suggest to you to do a thorough inspection of the frame. You can also an actuator test (without propellers) to make sure the motor output seems smooth, at least when you are not flying.

                                When I looked at the original log with the crash, it seemed to me that the gyro vibrations were a bit high, resulting in motor outputs to be noisy as well. Perhaps after a crash something changed (became more loose) and the vibration worsened, pushing the performance past the point of stability.

                                Please make sure that any cables that connect to VOXL2 are not tight, which can cause vibration to travel via cables or even pull on the cables if another component is loose on the frame.

                                I am not sure how much PID tuning you have done, but if the D gain on attitude control is set too high with noisy gyro, this will cause the noisy motor commands to be sent to motors.

                                A Offline
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                                Aaky
                                Regular
                                wrote on last edited by
                                #43

                                @Alex-Kushleyev Yes you were right. Problem was not with M0065 controling the motor. We got our vibrations sorted with good dampeners and now our drone flies well. Thank you! 🙂

                                Alex KushleyevA 1 Reply Last reply
                                0
                                • A Aaky

                                  @Alex-Kushleyev Yes you were right. Problem was not with M0065 controling the motor. We got our vibrations sorted with good dampeners and now our drone flies well. Thank you! 🙂

                                  Alex KushleyevA Online
                                  Alex KushleyevA Online
                                  Alex Kushleyev
                                  ModalAI Team
                                  wrote on last edited by
                                  #44

                                  @Aaky Great!

                                  One advice: save a few logs of good flights for future reference. In future, if something goes bad, you can go back and look at the old logs vs new logs and compare the amount of vibration, actuator outputs, etc.

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                                  • Alex KushleyevA Alex Kushleyev referenced this topic on
                                  • Alex KushleyevA Alex Kushleyev

                                    @Aaky Great!

                                    One advice: save a few logs of good flights for future reference. In future, if something goes bad, you can go back and look at the old logs vs new logs and compare the amount of vibration, actuator outputs, etc.

                                    A Offline
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                                    Aaky
                                    Regular
                                    wrote on last edited by Aaky
                                    #45

                                    @Alex-Kushleyev Yes Alex Noted.

                                    We were flying okish since last few days and we had another crash similar to last one. While we are seeing into our propulsion system design (motor propeller and battery), Aircraft this time flipped midair and the reason is absolutely unknown. I just wanted to eliminate if PWM outputs were given correctly to motors from M0065 in below shown flight while it crashed towards the end? I just wanted to check if PWM outputs were all above 1100 and none of the motor was commanded below the same. My VOXL2_IO_MIN and MAX are 1100 and 2000 respectively. Just eliminating any software problem over here once again. Let me know if you can help 🙂

                                    Log : https://review.px4.io/plot_app?log=d9d7feb3-9e5a-469f-ac95-a4914a243fbe

                                    Alex KushleyevA 1 Reply Last reply
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                                    • A Aaky

                                      @Alex-Kushleyev Yes Alex Noted.

                                      We were flying okish since last few days and we had another crash similar to last one. While we are seeing into our propulsion system design (motor propeller and battery), Aircraft this time flipped midair and the reason is absolutely unknown. I just wanted to eliminate if PWM outputs were given correctly to motors from M0065 in below shown flight while it crashed towards the end? I just wanted to check if PWM outputs were all above 1100 and none of the motor was commanded below the same. My VOXL2_IO_MIN and MAX are 1100 and 2000 respectively. Just eliminating any software problem over here once again. Let me know if you can help 🙂

                                      Log : https://review.px4.io/plot_app?log=d9d7feb3-9e5a-469f-ac95-a4914a243fbe

                                      Alex KushleyevA Online
                                      Alex KushleyevA Online
                                      Alex Kushleyev
                                      ModalAI Team
                                      wrote on last edited by Alex Kushleyev
                                      #46

                                      @Aaky ,

                                      I took a look at the log, the case seems a bit complicated. It seems the issue starts 6:38:500 when there is a sudden jerk that appears in Roll Rate, see here :
                                      c504e1c1-234b-4bb3-bc08-f233b0f3fb94-image.png

                                      As a a result, the vehicle tries to counter act and responds in actuator outputs (negative roll command to counteract the positive roll rate spike)

                                      4c04d157-6c2e-4c6a-bf54-f4f6da4aa8df-image.png

                                      This causes a sudden change in requested motor commands:
                                      80012099-329b-4869-a396-7adf19325563-image.png

                                      After that the vehicle starts oscillating and motor outputs are saturated. To me, it is unclear where the spike in the roll angular rate comes from after very low-noise fligiht. It is almost if something suddenly got loose, snapped, or hit the flight board, causing that angular rate spike. If the flight board became loose, it would have been impossible to stabilize the vehicle after that.

                                      Since you are using 3rd party ESCs, we do not have motor feedback, so we cannot tell if the motors performed well, but it does not look like the motors stopped, as the vehicle appears to start oscillating back and forth in roll initially. Also, if one or more motors simply stopped, we would have a smooth tumble - instead we are seeing a high roll rate impulse that seems to case oscillations and then the crash.

                                      I would suggest to inspect the vehicle and look for potential sources of that initial roll rate jerk that may have caused the oscillations and then crash.

                                      Alex

                                      Alex KushleyevA 1 Reply Last reply
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                                      • Alex KushleyevA Alex Kushleyev

                                        @Aaky ,

                                        I took a look at the log, the case seems a bit complicated. It seems the issue starts 6:38:500 when there is a sudden jerk that appears in Roll Rate, see here :
                                        c504e1c1-234b-4bb3-bc08-f233b0f3fb94-image.png

                                        As a a result, the vehicle tries to counter act and responds in actuator outputs (negative roll command to counteract the positive roll rate spike)

                                        4c04d157-6c2e-4c6a-bf54-f4f6da4aa8df-image.png

                                        This causes a sudden change in requested motor commands:
                                        80012099-329b-4869-a396-7adf19325563-image.png

                                        After that the vehicle starts oscillating and motor outputs are saturated. To me, it is unclear where the spike in the roll angular rate comes from after very low-noise fligiht. It is almost if something suddenly got loose, snapped, or hit the flight board, causing that angular rate spike. If the flight board became loose, it would have been impossible to stabilize the vehicle after that.

                                        Since you are using 3rd party ESCs, we do not have motor feedback, so we cannot tell if the motors performed well, but it does not look like the motors stopped, as the vehicle appears to start oscillating back and forth in roll initially. Also, if one or more motors simply stopped, we would have a smooth tumble - instead we are seeing a high roll rate impulse that seems to case oscillations and then the crash.

                                        I would suggest to inspect the vehicle and look for potential sources of that initial roll rate jerk that may have caused the oscillations and then crash.

                                        Alex

                                        Alex KushleyevA Online
                                        Alex KushleyevA Online
                                        Alex Kushleyev
                                        ModalAI Team
                                        wrote on last edited by
                                        #47

                                        Even though it is not clear what the initial roll rate spike came from, it seems that it served as an impulse test of the attitude controller and the vehicle started oscillating. If nothing actually came loose during the flight, this may suggest that your attitude controller is not stable and given an large disturbance it can become unstable. There are many unknown variables, but you may need to increase your D gain in your attitude controller to dampen the response. However, still, it is still not clear where the original roll rate impulse came from here..

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                                        • Alex KushleyevA Alex Kushleyev

                                          Even though it is not clear what the initial roll rate spike came from, it seems that it served as an impulse test of the attitude controller and the vehicle started oscillating. If nothing actually came loose during the flight, this may suggest that your attitude controller is not stable and given an large disturbance it can become unstable. There are many unknown variables, but you may need to increase your D gain in your attitude controller to dampen the response. However, still, it is still not clear where the original roll rate impulse came from here..

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                                          Aaky
                                          Regular
                                          wrote on last edited by
                                          #48

                                          @Alex-Kushleyev Thanks for your analysis Alex. This is somewhat a mystery for us as well. Actually in terms of motor saturation, I feel motor saturation started first at timestamp 6:38:560 onwards motors had started to struggle leading to roll failure. We are suspecting if propeller broke in flight, since it was not in our visual sight flying 200 meters away. We flew with another set of propeller at very high speed again and things were all normal this time. There isn't any concrete answer to this just speculations as of now.

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