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    How to: Seeker ESC calibration

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    • A
      alarm_hq
      last edited by

      I'm unsure how to calibrate the ESCs on the seeker.

      I can't use qgroundcontrol as the seeker doesn't have 5v input, non battery power input as documented here

      However, using the px4-esc-tool to calibrate the seeker's ESC, the prompts request your to remove J1007 from the VOXL Flight. This connector is not populated from the factory.

      Any advice? Should I just ignore it and move to the next step?

      1 Reply Last reply Reply Quote 0
      • Chad SweetC
        Chad Sweet ModalAI Team
        last edited by

        There is no need to calibrate the Seeker's ESC. They use a closed loop RPM control with parameters specified at the factory.

        So we can improve our documentation, where is that step listed?

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        • Chad SweetC
          Chad Sweet ModalAI Team
          last edited by

          The Seeker (and all of our drones), come ready to fly out of the box.

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          • A
            alarm_hq
            last edited by

            And if I've already made the "mistake" of reflashing px4 firmware, is the closed loop RPM control affected?

            James StrawsonJ 1 Reply Last reply Reply Quote 0
            • Chad SweetC
              Chad Sweet ModalAI Team
              last edited by

              Ah 🙂 I'll ping some more folks. Don't know off the top of my head.

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              • modaltbM
                modaltb ModalAI Team
                last edited by

                Mainline PX4 doesn't have our ESC driver (yet), so if was from the QGC auto update, it's likely wiped that driver out!

                Here's the .px4 binary that has support (what we are shipping with).

                info:
                https://docs.modalai.com/flight-core-firmware/

                v1.11.3-0.0.5:
                https://storage.googleapis.com/modalai_public/flightcore-releases/1.11.3-0.0.5.modalai_fc-v1_default.px4

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                • modaltbM
                  modaltb ModalAI Team
                  last edited by

                  Source code for reference: https://github.com/modalai/px4-firmware/tree/modalai-1.11/src/drivers/uart_esc/modalai_esc

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                  • A
                    alarm_hq
                    last edited by

                    Awesome, that was the driver I had used. Thanks for clarifying!

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                    • James StrawsonJ
                      James Strawson ModalAI Team @alarm_hq
                      last edited by

                      @alarm_hq said in How to: Seeker ESC calibration:

                      And if I've already made the "mistake" of reflashing px4 firmware, is the closed loop RPM control affected?

                      The ModalAI ESCs used on Seeker have their own firmware and settings stored on the ESC itself, independent from PX4 so your ESC is fine after changing PX4 firmware.

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