Starling 2 - failure when entering offboard mode in Starling 2
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Hello,
After fresh IMU and gyro calibration, and with successful check of VIO (via VOXL portal) Starling 2 is able to arm in position mode and fly in position mode rather well. However, as soon as switching to offboard mode (in this case to test follow_tag) flight becomes unstable: drone starts to very quick climbing straight up in the vertical direction.
It seems this kind of failure (drone starts climbing up fast straight in the vertical direction) seems a relatively common failure mode when going to offboard mode. Are there any suggestions of what can be causing this ? VIO has been tested multiple times and looks solid. Drone is able to arm in position mode.
Please let me know your suggestions. Thanks.