M500 heading issues
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With one of our M500 drones with the VOXL flight deck is having heading issues. The vehicle is reporting a heading that is around 90 degrees off from where it should be.
No amount of compass calibrations would rectify this, and there are no ferrous obstructions near the compass that would interfere. Any ideas as to what could be causing this issue?Here is a link to a flight: https://drive.google.com/file/d/1Qpf8b7SfiQASRapk-oUV_BNncVn3OTNh/view?usp=share_link
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The Holybro GPS module has the magnetometer rotated
Any chance the Mag rotation parameter was changed on accident?
See the factory parameters here: https://gitlab.com/voxl-public/flight-core-px4/px4-parameters/-/tree/master/platforms/v1.13/M500
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The Holybro GPS module has the magnetometer rotated
Any chance the Mag rotation parameter was changed on accident?
See the factory parameters here: https://gitlab.com/voxl-public/flight-core-px4/px4-parameters/-/tree/master/platforms/v1.13/M500
@Chad-Sweet Looks like it was set to "no rotation." So it looks like the parameter had been changed accidentally. Looking at the parameter list, do I set the orientation to 10 or 6?
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Please refer to the M500 factory parameters here: https://gitlab.com/voxl-public/flight-core-px4/px4-parameters/-/tree/master/platforms/v1.13/M500
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