I have had several successful flights with our Seeker. No hardware or software changes.
Last several attempts (spaced out over a week) have failed. The front left landing gear never leaves the ground. When the throttle is pushed to 75% in manual mode the Seeker will start to spin in circles around the front left motor.
I have pulled PX4 ULG logs and plotted them with PlotJuggler.
Motor actuator and ESC RPMs show that 1 motor (or ESC) spins up almost none. I can upload this data, but I dont seem to be able to attach to this post.
I can buy a replacement motor from GetFpv. I assume I would need a quote for a Modal AI ESC?