@Alex-Kushleyev m/s/s
Posts made by Sasha Bagan
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IMU is extremely noisy
We've recently purchased starling 2 drone and are having issues executing even simple flights (takeoff with RC and flying in position mode), we've triaged those issues to the imu. Once VIO gets enough features the drone becomes more stable but generally taking off in position mode often fails. We've recorded imu data via voxl-logger (200hz, --skip 4) and the chart looks extremely noisy
We've also tried recalibrating IMU (voxl-calibrate-imu-temp and voxl-calibrate-imu). Could it be that the IMU sensor is damaged? What next steps would you recommend?